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Test Flight Update
December 16, 1996
The following is Virgin's written account of the follow-up analysis of the
November 9th test flight:
The follow up analyses to the November 9th test flight shows that the
preliminary speculations of fabric leakage of helium or a misfitted rip panel
were not correct. The integrity of the balloon and its fabric were further
proven to be flight-line ready during a subsequent flight. The following week,
the same balloon, with no modifications, was inflated and attached to a gondola
designed for a high altitude test. It not only completed the test but broke all
previous world records for altitude in this type of balloon. (See Newsflash:
Lindstrand Breaks Altitude Record)
The original low altitude test flight, using a very large and heavily
weighted basket, was conducted to test various components that will be
used on the Global Challenger flight. Included was the data collection
system which proved to be extremely accurate and revealed the reasons
for the shortened flight time. Other items included the gas valve that
will be used for the global flight and an instrument that measures
reflected versus absorbed sunlight. The flight was specifically designed
to test the balloon's performance and fuel consumption under the least
desirable weight conditions.
A De Rozier balloon combines gas balloon and hot air balloon methods,
allowing the flight crew to keep the temperature of the helium constant
during day and nighttime temperatures. The goal is to prevent the helium
from contracting as it cools which in essence produces a smaller
balloon. Naturally, a balloon that becomes effectively smaller while
carrying the same weight, will begin to sink. Therefore, the test
balloon, with a heavier basket and three people on board, required a
great deal of fuel to keep it aloft. (A more detailed explanation of
the workings of a De Rozier balloon system can be found elsewhere on
this web site.)
The flight was shortened for two reasons. First, that the effectiveness of
the Lindstrand heating system surpassed the flight crew's expectations.
The helium expanded to such an extent that it repeatedly vented though
the overfill appendix tube. The tube is designed to relieve internal pressure
in the balloon as the helium expands by allowing the helium to escape. For the
global flight, this venting will be minimal because it will be limited
to that which occurs naturally as the balloon reaches its ceiling
altitude and not through the over use of the heaters. However, in the
case of the November 9 test flight, the loss of helium meant loss of
flight time.
The second reason for the abbreviated flight was that the wind was
taking the balloon into territory where a quick retrieval would be
unlikely and potential damage to the craft would preclude the more
important high altitude flight. To that end, just before dark and before
they reached the next mountain range, the crew elected to
land while over a valley with dirt roads.
(previous newsflash)
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